留言板

尊敬的读者、作者、审稿人, 关于本刊的投稿、审稿、编辑和出版的任何问题, 您可以本页添加留言。我们将尽快给您答复。谢谢您的支持!

姓名
邮箱
手机号码
标题
留言内容
验证码

环形防喷器卡阻试压塞事件解析与预防

Analysis and prevention of annular BOP jamming test plug event

  • 摘要: 某半潜式钻井平台钻探作业中,对水下防喷器组完成试压后,出现试压塞起出受阻问题。在处理问题的过程中,发生环形防喷器胶芯严重卡阻试压塞事件,导致平台长时间停待。文章回顾事件的发生和处理过程,通过对事件中出现的各种现象、迹象的解析,指出试压塞起出受阻和被环形防喷器严重卡阻的原因。结合原因分析及对相关资料的调研,该文提出了防止类似事件再次发生的预防措施,供相关从业者借鉴。

     

    Abstract: During the drilling operation of a semi-submersible drilling platform, after the pressure test on the subsea blowout preventer (BOP) stack was completed, a problem occurred where the test plug could not be pulled out smoothly. In the process of handling this issue, a serious jamming of the test plug by the rubber core of the annular blowout preventer happened, resulting in a long-term shutdown of the platform. This article reviews the occurrence and handling process of the incident, identifies the causes of the test plug's difficulty in being pulled out and its serious jamming by the annular blowout preventer through analyzing various phenomena and signs in the incident. Based on the cause analysis and the study of relevant materials, the paper puts forward preventive measures to avoid similar incidents, providing a reference for relevant practitioners.

     

/

返回文章
返回