CHEN Lei, ZHAO Jian, SHEN Jinwei, LI Meng, GUO Bumin, JIN Jiyun. Development and Evaluation of Safety Depolymerizer for Polymer Injection Wells in JZ9-3 Oilfield[J]. Offshore oil, 2020, 40(1): 65-69. DOI: 10.3969/j.issn.1008-2336.2020.01.065
Citation: CHEN Lei, ZHAO Jian, SHEN Jinwei, LI Meng, GUO Bumin, JIN Jiyun. Development and Evaluation of Safety Depolymerizer for Polymer Injection Wells in JZ9-3 Oilfield[J]. Offshore oil, 2020, 40(1): 65-69. DOI: 10.3969/j.issn.1008-2336.2020.01.065

Development and Evaluation of Safety Depolymerizer for Polymer Injection Wells in JZ9-3 Oilfield

  • In view of the plugging problem caused by long-term polymer injection of JZ9-3 oilfield, the composition and characteristics of the blockage in well W are analyzed. A safety depolymerizing agent was developed by the screening and optimization of oxidizer and stabilizer, and the performance evaluation of plugging corrosion, one-dimensional sand-filled pipe model displacement experiments and corrosion rate were carried out. The experimental results showed that percarbonamide can reduce the viscosity rate of high-concentration polymer solutions and gels by up to 99%.After adding a stabilizer, the release rate of active oxygen can be controlled, and it can still maintain 8% active oxygen content at 60℃ after 72 h, which greatly improves the safety of depolymerizer. The blockage removal rate of the depolymerizer is 91.6%, and the permeability recovery rate is 305%. The depolymerizer has the characteristics of low corrosion rate and no oxygen generation, so as to ensure the safety of on-site operation. The application of the depolymerizer in W well shows that it can effectively remove the blockage caused by long-term polymer injection.
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