留言板

尊敬的读者、作者、审稿人, 关于本刊的投稿、审稿、编辑和出版的任何问题, 您可以本页添加留言。我们将尽快给您答复。谢谢您的支持!

姓名
邮箱
手机号码
标题
留言内容
验证码
邱康, 雷新超, 贾凤龙, 马帅. 氯化钾聚合醇钻井液在涠西区块定向井应用效果分析[J]. 海洋石油, 2016, 36(3): 93-97. DOI: 10.3969/j.issn.1008-2336.2016.03.093
引用本文: 邱康, 雷新超, 贾凤龙, 马帅. 氯化钾聚合醇钻井液在涠西区块定向井应用效果分析[J]. 海洋石油, 2016, 36(3): 93-97. DOI: 10.3969/j.issn.1008-2336.2016.03.093
QIU Kang, LEI Xinchao, JIA Fenglong, MA Shuai. Analysis of Application Results of Potassium Chloride/Polyglycol Drilling Fluid Systems Used in Directional Well in Weixi Block[J]. Offshore oil, 2016, 36(3): 93-97. DOI: 10.3969/j.issn.1008-2336.2016.03.093
Citation: QIU Kang, LEI Xinchao, JIA Fenglong, MA Shuai. Analysis of Application Results of Potassium Chloride/Polyglycol Drilling Fluid Systems Used in Directional Well in Weixi Block[J]. Offshore oil, 2016, 36(3): 93-97. DOI: 10.3969/j.issn.1008-2336.2016.03.093

氯化钾聚合醇钻井液在涠西区块定向井应用效果分析

Analysis of Application Results of Potassium Chloride/Polyglycol Drilling Fluid Systems Used in Directional Well in Weixi Block

  • 摘要: 针对涠西区块复杂井段钻井液的使用要求,基于涠西区块定向井钻井施工现象,对氯化钾聚合醇钻井液在该区域定向井应用效果进行了分析,结果表明:氯化钾聚合醇钻井液能够基本满足涠西区块定向井钻井施工要求,但没有彻底解决涠二段到流二段井壁垮塌问题,需要进一步对钻井液体系及性能进行优化,以便更好地解决复杂井段井壁垮塌问题,确保后续定向井及水平井钻井施工安全。

     

    Abstract: To meet the requirements for drilling fluid used in complex interval of Weixi block, based on drilling phenomenon of directional well, the application results of potassium chloride/polyglycol drilling fluid system is analyzed for directional well in Weixi block. The study results show that potassium chloride/polyglycol drilling fluid system can meet basically the requirements for drilling directional well in Weixi block. However, the wellbore collapse problem from Wei-2 to Liu-2 Members has not solved completely. Further study and optimization should been conducted to solve complex well borehole collapse problem, and ensure the subsequent operation safety of directional wells and horizontal wells.

     

/

返回文章
返回